| dc.contributor.author | UMAM, Alfan Khoirul |  | 
| dc.date.accessioned | 2024-07-16T02:09:50Z |  | 
| dc.date.available | 2024-07-16T02:09:50Z |  | 
| dc.date.issued | 2023-07-28 |  | 
| dc.identifier.nim | 191910801015 | en_US | 
| dc.identifier.uri | https://repository.unej.ac.id/xmlui/handle/123456789/122336 |  | 
| dc.description.abstract | Field "R" is an old field located in the South East Sumatra Block. The pipeline 
network in Area "WK-1" in field "R" has 8 platforms namely the RAMB, RAMD, 
RAMI, SWWA, WANA, NWAA, GITA, and RAMC. There are 31 producing wells 
through the 8 platforms. The purpose of this research is to create a piping network 
model for Area "WK-1" Field "R", identify optimal or non-optimal conditions for 
pipelines through simulation results and matching on the pipeline network model,
identify whether bottlenecking problems occur in the piping network Area "WK-1" 
Field "R" using the matching results on the piping network model so that the 
location of pipes and nodes with fluid problems can be found precisely, and carry 
out production optimization simulations to increase production rates oil in Area 
"WK-1" Field "R". Production well modeling and pipeline network modeling using 
a multiphase steady-state production simulator application, the models that have 
been made will be validated matching against actual conditions. From the results 
of matching the pipe network model, an analysis of pipe problems that can occur 
such as bottlenecks is carried out. From the network simulation results, it can be 
seen that there is bottlenecking on the pipeline in Area "WK-1" Field "R". From the 
simulation results, there are 2 optimization scenarios, the production capacity of 
each well can still be increased and the total rate of oil production increases. In the 
first scenario, setting the bean size on the choke, the oil flow rate increases by 48.92 
BOPD with an average increase of 1.55%. Whereas in the second scenario, by 
opening the pressure limits at the wellhead points, the result is an increase in the 
oil flow rate of 583.25 BOPD with an average increase of 16.13%. | en_US | 
| dc.language.iso | other | en_US | 
| dc.publisher | Fakultas Teknik | en_US | 
| dc.subject | Bottlenecking | en_US | 
| dc.subject | Pipelines | en_US | 
| dc.subject | Optimization | en_US | 
| dc.title | Evaluasi Jaringan Pipa Minyak Lepas Pantai Guna Optimasi Produksi Area "WK-1" Lapangan "R" | en_US | 
| dc.type | Other | en_US | 
| dc.identifier.prodi | Teknik Perminyakan | en_US | 
| dc.identifier.pembimbing1 | Hadziqul Abror, S.Si., M.T. | en_US | 
| dc.identifier.pembimbing2 | Riska Laksmita Sari S.Si., M.T. | en_US | 
| dc.identifier.validator | validasi_repo_iswahyudi_Mei_2024 | en_US | 
| dc.identifier.finalization | 0a67b73d_2024_07_tanggal 10 | en_US |